Cost Reduction in the Accumulator Process in Welding Operations
Zusammenfassung
For the last few weeks, the heating,
ventilation, and air conditioning manufacturing
company Thermo King Arecibo has been increasing
the operational cost due to leak problems on the
accumulator area in the welding department. The
purpose of this project is to find the root cause of
the problem causing this increase in defects in
order to reduce budgeted cost while maintaining
compliance with ISO regulation. Under this
panorama the welding department of Thermo King
Arecibo determines to look into the process using
concept that combined Lean manufacturing
techniques and Six Sigma tools and strategies. This
Lean Six Sigma Methodology focused on business
and process improvements based on decrease of
process variation, waste elimination, process
improvement and customer satisfaction. This
project has been developed under the Lean Six
Sigma principles and using DMAIC five-step
approach, in order to identify opportunities to
enable the company to reduce overall cost and gain
efficiencies and breakthrough the welding
department operation cost. The plan
implementation helped reduce waste by 6.0%,
resulting in a saving of more than $3,259.64 per
month. As part of the implementation
sustainability, a sheet maintenance schedule (SMS)
for the robot was created in order to minimize leaks
defects due to poor maintenance of the robot.
Key words: Accumulator, Lean, Waste,
Welding.