Application of Lean Manufacturing and Lean Six Sigma Tools to Improve Back to Back Activities in the Compression Process
Resumen
A recent opportunity regarding a
product ramp up in the production schedule due to
a potential product transfer requires the
manufacturing area to look for creative ways to
improve in order to comply with expected demand.
By applying Lean Six Sigma concepts, the current
process was defined, a baseline was established,
and improvements were identified and executed.
The results achieved due to these improvements
were: average back to back cycle time in the
compression area was reduced from an average of
3.7 hours to 2.87 hours for a 22% reduction and a
standard deviation reduction of 91% (1.44 to 0.131
hours). These results were achieved by
implementing parallel activities as well as
eliminating constraints (redundant documentation
and availability of tools) throughout the process.
The improvements were also instrumental in
achieving a potential capacity increase of an
additional 1.33 lots for a work week due to
additional time available.
Key Terms ⎯ Baseline Establishment, Cycle
Time, Improvements, Lean Manufacturing.