Production Line Improvement Using DMAIC Tool in an Electrical Production Plant
Resumen
Today, there is much competition between
the manufacturers of electronics products. This
creates a need for the manufacturers to develop
processes that can supply the client demand within
a required time and a specified quality. The studied
production line had productivity problems, since it
was never able to reach the 95% productivity level
established by the company, and had a backorder
cost of $26K. These factors affected the availability
of products required by the customer. Using the
DMAIC tool the main factors that affected the
production output were properly identified to
correct the problem of a production line that did
not meet adequately the client demand. The initials
stand for: Define Measurement, Analyze, Improve
and Control. As a result of working with causes
affecting the productivity problems of the studied
area, the productivity was increased from 85% to
96.7% and Backorder costs were reduced to
$4,300.
Key Terms: DMAIC, Sub. assemblies, Molding
Parts, 5’S.